Fix It Again Tony

Illustration for article titled Fix It Again Tony

As you may have gathered if you’ve been reading along with my Welsh adventure, I may or may not have put my little X1/9 through a hedge. Not cool. Still, we can rebuild it! We have the technology :)

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First thing’s first, a damage assessment:

  • Front end pretty thoroughly mashed in and cut up to get the bonnet open
  • Various dings all over the body
  • Left-hand tie rod bent to 45-degrees (fixed in Wales)
  • Couldn’t quite get the tracking right in Wales which suggests something else is bent
  • Front left wheel which took the brunt of the force seems to rock back and forth on the strut (the rod of the shock moves in relation to the body)
  • Radiator pushed back 4", but otherwise intact
  • Lower lip spoiler pulled off
  • Bumpers wrecked
  • Wing mirror left behind in the field
  • Fuel pump whining and not able to keep up with fuelling above 4000rpm towards the end of the trip
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Next up, lets strip everything down ready for repair (exposing just how thoroughly wrecked the nose panel is).

Not pretty...
Not pretty...
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Then removing all of the mangled metal and welding it back up. Had to cut a slit along the top of the bent section to pull it down and forwards into shape, and re-make the leading lip.

Illustration for article titled Fix It Again Tony
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Apologies for the schizophrenic photo brightness. This was done over the course of a few days.
Apologies for the schizophrenic photo brightness. This was done over the course of a few days.

As a thankyou for borrowing the MG F, my mate bought me a fibreglass nosecone as you can’t really get steel ones anymore. Took a bit of fettling to get it into the right shape (slit down the middle and bent up slightly), but got there in the end.

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Illustration for article titled Fix It Again Tony
Illustration for article titled Fix It Again Tony
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Before:

Illustration for article titled Fix It Again Tony
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After:

Illustration for article titled Fix It Again Tony
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Next step was to sort the rad. Not that it really needed extra cooling at the moment, but in the future I’d like to see if I can push the power up a little on this so an alloy rad would be a good investment :)

Difficult to find in the UK, but I found an outfit in the States selling some really nice ones. Trouble is they were quoting about £200 in shipping!

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Now, if anyone’s been knocking around here for long enough they’ll remember a bit of an exodus when the forums switched over to kinja. I still buzz about the G+ forum where the refugees live, and a brilliant lady there helped me out with shipping :) can’t remember her oppo handle, but she has a dark green ‘70s Charger ad saved me a bucketload of cash sending this thing over:

Illustration for article titled Fix It Again Tony
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Supposed to be bolt-on, but it fouled the original radiator bracket so I took the opportunity to make a lightweight tubular one :)

These little magnetic triangles are brilliant bits of kit :)
These little magnetic triangles are brilliant bits of kit :)
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Illustration for article titled Fix It Again Tony

And fitted :)

Illustration for article titled Fix It Again Tony
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Ok, now for the dings and bent suspension. I was originally going to get some quotes for paintless dent repair, but then I thought ‘I’ve got a rubber mallet and a block of 4x2...how hard can it be?’.

Turns out, not that difficult.

Illustration for article titled Fix It Again Tony
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Gutted I didn’t get a before pic, but there used to be a massive dent on the rear part of this wing. Pushed in a good half-inch over a dinner-plate-sized area. Just look at the reflection of the bin in it now. Flat as a pancake ;)

There’s still some wrinkles at the back where I couldn’t get the mallet behind properly, and below where there’s a complicated little crease, but it’s about a billion times better than it used to be.

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As for suspension, you can see in this pic on the lower right where the forward suspension link has been pulled downwards by the impact:

The gap you can see at the back in between the two downward prongs and the radiator mount bar.
The gap you can see at the back in between the two downward prongs and the radiator mount bar.
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Jacked that up and welded it back together. I also discovered the big ol’ cast steel transverse link was tweaked a bit. Expensive buggers to replace, so I carefully straightened it out in my pipe bender which worked a treat :)

The knocking shock/strut turned out to be the shock insert moving inside the strut. Further inspection showed that the big threaded section that clamps the shock in had been expanded slightly by the impact so that it would slip if you tried to screw it in tight enough to hold it steady.

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After a bit of an abortive search for replacement struts I decided to fix that too. Stuck it in the vice with a big beefy socket beneath it (securing it on 3 sides) and the top bit screwed in. Then proceeded to ‘tap’ it with a big lump hammer progressively around and around the outside shrinking it until you could bolt it up ok. Again, worked a treat :)

Next thing I noticed was that the coolant pipes running along the front of the car were leaking a bit. Fair amount of faffing about to get them sealed, but eventually I made these :)

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Illustration for article titled Fix It Again Tony
Illustration for article titled Fix It Again Tony
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Hum, what was next? Oh yeah, bumpers. I’d picked up some fibreglass replacement ones but they came without mounting hardware so made up some little brackets and rubber mounts to fit them to the body and fibreglassed them in place.

Illustration for article titled Fix It Again Tony
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Illustration for article titled Fix It Again Tony

Discovered that the whining fuel pump was due to a thoroughly blocked filter. Replaced that (and the pump for good measure) and the running problems sorted themselves :)

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Noticed that the handbrake probably wouldn’t pass MoT so set about adjusting that. Had to widen the access panel underneath the car as the new coolant hose routing at the back ran directly over the old access hole.

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Adjsutment didn’t really fix it as they didn’t seem to be releasing properly, so took the calipers apart to have a look why. Glad I did as this is what came out:

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Some of those chunks of rust are a good few millimetres in diameter. Plenty enough to get stuck in brake pipes. We reckoned the master cylinder had probably gone rusty inside as it was pretty rusty outside so set about replacing that. Right pain in the backside job that. Who puts a brake master cylinder in the driver’s footwell?

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Replaced that (somehow managing to avoid spilling brake fluid all over the footwell which was a minor miracle). Also resealed all the brakes while I was at it to check that they didn’t have buckets of rust inside them too. Bleeding them was a pain as one of the banjo fittings wasn’t sealing properly. The only way we found out is that when someone leant on the pedal quite hard it sent a jet of brake fluid across the garage. Some better quality copper washers fixed that.

And this is how she stands now!

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She would be ready for MoT if the horn hadn’t inexplicably stopped working. Wouldn’t be that irritating if we hadn’t already fixed it once before.

Still a couple of bits and pieces to fix (tappy valves, bigger rear calipers from a Lancia Montecarlo to balance the brakes better, and a weakly charging alternator), but nothing I can’t do as I’m driving :)

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So yeah. Nearly there! I can’t wait :)